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g down with it and resulting in a number of badly broken plates in the bottom of the rings. Notwithstanding the use of extremely high vertical leads,[D] the sand was so soft that the settlement of the shield continued for about fifteen rings, the maximum being nearly 9 in. below grade. The hydrostatic head at mid-height of the tunnel was 32-1/2 lb., and the raising of the air pressure to 37 lb., as was done at this time, was attended with grave danger of serious blows, on account of the recent disturbance of the natural cover by the pulling and re-driving of piles in the reconstruction of the Long Island ferry slips directly above. It dried the face materially, however, and the shield began to rise again, and had practically regained the grade when the anticipated blow-outs occurred, culminating with the entrance of rip-rap from the river bed into the shield and the flooding of the tunnel with 4 ft. of sand and water at the forward end. The escape of air was very great, and, as a pressure of more than 28 lb. could not be maintained, the face was bulkheaded and the tunnel was shut down for three weeks in order to permit the river bed to consolidate. This was the most serious difficulty encountered on any part of the work, and, coming at the very start, was exceedingly discouraging. During the shut-down the broken plates were reinforced temporarily with steel ribs and reinforced concrete (Fig. 1, Plate LXXIII) which, on completion of the work, were replaced by cast-steel segments, as described elsewhere. Practically, no further movement of iron took place, and the loss of grade caused by the settlement of the shield, which was by far the largest that ever occurred in this work, was not sufficient to require a change in the designed grade or alignment of the track. Work was resumed with the shutters in use at the face as an aid to excavation. The features of extreme seriousness did not recur, but for two months the escape of air continued to be extremely large, an average of 15,000 cu. ft. per min. being required on many days during this period. [Illustration: PLATE LXXIII, FIG. 1.--TEMPORARY REINFORCEMENT OF BROKEN PLATES AND REMOVAL OF A PLATE IN SECTIONS.] [Illustration: PLATE LXXIII, FIG. 2.--HEAVY CAST-STEEL PATCH ATTACHED TO BENT SEGMENT OF CUTTING EDGE.] [Illustration: PLATE LXXIII, FIG. 3.--INFLOW OF SOFT CLAY THROUGH SHIELD.] [Illustration: PLATE LXXIII, FIG. 4.--REINFORCEMENT OF BROKEN PLATE WITH LONG
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