FREE BOOKS

Author's List




PREV.   NEXT  
|<   39   40   41   42   43   44   45   46   47   48   49   50   51   52   53   54   55   56   57   58   59   60   61   62   63  
64   65   66   67   68   69   70   71   72   73   74   75   76   77   78   79   80   81   82   83   84   85   86   87   88   >>   >|  
first that the proper method would be a complete heat treatment of the forging in the rough state, and machining the rod after the heat treatment. After a number of trial lots, the Signal Corps acceded to the request and production was immediately increased and quality benefited by the change. This method was later included in a revised specification issued to all producers. The original system was one that required a great deal of labor per unit output. The Lincoln organization developed a method of handling connecting rods whereby five workmen accomplished the same result that would have required about 30 or 32 by the original method. Even after revising the specification so as to allow complete heat treatments in the rough-forged state, the ordinary methods employed in heat-treating would have required 12 to 15 men. With the fixtures employed, five men could handle 1,300 connecting rods, half of which are plain and half, forked, in a working period of little over 7 hr. [Illustration: Fig. 14.--Rack for holding rods.] [Illustration: Fig. 15.--Sliding rods into tank.] The increase in production was gained by devising fixtures which enabled fewer men to handle a greater quantity of parts with less effort and in less time. In heat-treating the forgings were laid on a rack or loop _A_, Fig. 14, made of 1-1/4-in. double extra-heavy pipe, bent up with parallel sides about 9 in. apart, one end being bent straight across and the other end being bent upward so as to afford an easy grasp for the hook. Fifteen rods were laid on each loop, there being four loops of rods charged into a furnace with a hearth area of 36 by 66 in. The rods were charged at a temperature of approximately 900 deg.F. They were heated for refining over a period of 3 hr. to 1,625 deg.F., soaked 15 min, at this degree of heat and quenched in soluble quenching oil. In pulling the heat to quench the rods, the furnace door was raised and the operator pulls one of the loops _A_, Fig. 15 forward to the shelf of the furnace, supporting the straight end of the loop by means of the porter bar _B_. They swung the loop of rods around from the furnace shelf and set the straight end of the loop on the edge of the quenching tank, then raise the curved end _C_, by means of their hook _D_ so that all the rods on the loop slide into the oil bath. Before the rods cooled entirely, the baskets in the quenching tank were raised and the oil allowed to partly d
PREV.   NEXT  
|<   39   40   41   42   43   44   45   46   47   48   49   50   51   52   53   54   55   56   57   58   59   60   61   62   63  
64   65   66   67   68   69   70   71   72   73   74   75   76   77   78   79   80   81   82   83   84   85   86   87   88   >>   >|  



Top keywords:

method

 

furnace

 
required
 

straight

 

quenching

 

period

 

Illustration

 

employed

 

treating

 
handle

fixtures
 

raised

 

charged

 
treatment
 
complete
 

production

 

connecting

 
original
 

specification

 
included

approximately

 
temperature
 
revised
 

heated

 

immediately

 

soaked

 
refining
 

Fifteen

 

producers

 
upward

hearth
 

degree

 

issued

 

afford

 

soluble

 

curved

 

allowed

 

partly

 

baskets

 
Before

cooled
 
change
 

operator

 

quench

 

pulling

 
proper
 

forward

 

porter

 

benefited

 

increased